David Price

Statoil alpha day2 files

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<witsml:drillReports version="1.4.0.0" xmlns:witsml="http://www.witsml.org/schemas/1series" xmlns:xsi="http://www.w3.org/2001/XMLSchema-instance" xsi:schemaLocation="http://www.witsml.org/schemas/1series http://www.npd.no/schema//DDRS/1series/WITSML_drillReport_profiled_schema_phase2.xsd"><witsml:documentInfo><witsml:documentName>Drill Report</witsml:documentName><witsml:owner>IIP</witsml:owner></witsml:documentInfo><witsml:drillReport><witsml:nameWell>NO 30/9-B-45</witsml:nameWell><witsml:nameWellbore>NO 30/9-B-45</witsml:nameWellbore><witsml:name>name</witsml:name><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:versionKind>normal</witsml:versionKind><witsml:createDate>2011-10-05T07:55:33.000Z</witsml:createDate>
<witsml:wellAlias><witsml:name>30/9-B-45</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellAlias>
<witsml:wellboreAlias><witsml:name>30/9-B-45</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellboreAlias><witsml:wellboreAlias><witsml:name>4513</witsml:name><witsml:namingSystem>NPD number</witsml:namingSystem></witsml:wellboreAlias>
<witsml:wellboreInfo><witsml:dTimSpud>2002-03-20T00:00:00.000Z</witsml:dTimSpud><witsml:operator>Statoil</witsml:operator><witsml:drillContractor>Aker Well Service</witsml:drillContractor><witsml:rigAlias><witsml:name>OSEBERG B</witsml:name><witsml:namingSystem>NPD Name</witsml:namingSystem></witsml:rigAlias><witsml:rigAlias><witsml:name>272897</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:rigAlias></witsml:wellboreInfo>
<witsml:statusInfo><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">8225</witsml:md><witsml:tvd uom="m">2716.3</witsml:tvd><witsml:diaHole uom="in">0</witsml:diaHole><witsml:mdDiaHoleStart uom="m">918</witsml:mdDiaHoleStart><witsml:mdKickoff uom="m">167</witsml:mdKickoff><witsml:tvdStrengthForm uom="m">0</witsml:tvdStrengthForm><witsml:mdPlanned uom="m">-9999</witsml:mdPlanned><witsml:distDrill uom="m">-9999</witsml:distDrill><witsml:elevKelly uom="m">58</witsml:elevKelly><witsml:sum24Hr>Intervention crew arrived platform.
Started to spot and check out wireline equipmen at BOP deck.</witsml:sum24Hr><witsml:forecast24Hr>Continue RU on BOP deck. Hook up equipment to platform power, F&amp;G etc.</witsml:forecast24Hr><witsml:ropCurrent uom="m/h">-9999</witsml:ropCurrent></witsml:statusInfo>
<witsml:extendedReport dTim="2011-10-04T00:00:00.000Z">Depth: 0. Rig crane still down due to heavy wind.
Continued spotting and hooking up equipment on BOP deck. </witsml:extendedReport >
<witsml:activity><witsml:dTimStart>2011-10-03T15:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T19:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Started to check out the arrived wireline equipment.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T19:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Rig crane down due to heavy wind.
Spotted equipment on BOP deck. Started to hook up cables and hoses between wl-winch and add-on unit.</witsml:comments></witsml:activity>
</witsml:drillReport></witsml:drillReports>
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<witsml:drillReports version="1.4.0.0" xmlns:witsml="http://www.witsml.org/schemas/1series" xmlns:xsi="http://www.w3.org/2001/XMLSchema-instance" xsi:schemaLocation="http://www.witsml.org/schemas/1series http://www.npd.no/schema//DDRS/1series/WITSML_drillReport_profiled_schema_phase2.xsd"><witsml:documentInfo><witsml:documentName>Drill Report</witsml:documentName><witsml:owner>IIP</witsml:owner></witsml:documentInfo><witsml:drillReport><witsml:nameWell>NO 30/9-F-7 A</witsml:nameWell><witsml:nameWellbore>NO 30/9-F-7 AT2</witsml:nameWellbore><witsml:name>name</witsml:name><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:versionKind>normal</witsml:versionKind><witsml:createDate>2011-10-05T07:56:05.000Z</witsml:createDate>
<witsml:wellAlias><witsml:name>30/9-F-7 A</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellAlias>
<witsml:wellboreAlias><witsml:name>30/9-F-7 AT2</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellboreAlias><witsml:wellboreAlias><witsml:name>6628</witsml:name><witsml:namingSystem>NPD number</witsml:namingSystem></witsml:wellboreAlias>
<witsml:wellboreInfo><witsml:dTimSpud>2011-09-24T00:00:00.000Z</witsml:dTimSpud><witsml:operator>Statoil</witsml:operator><witsml:drillContractor>KCA Deutag Drilling Norge AS</witsml:drillContractor><witsml:rigAlias><witsml:name>OSEBERG SØR</witsml:name><witsml:namingSystem>NPD Name</witsml:namingSystem></witsml:rigAlias><witsml:rigAlias><witsml:name>280205</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:rigAlias></witsml:wellboreInfo>
<witsml:statusInfo><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">1603</witsml:md><witsml:tvd uom="m">1371.64</witsml:tvd><witsml:diaHole uom="in">17.5</witsml:diaHole><witsml:mdDiaHoleStart uom="m">1204</witsml:mdDiaHoleStart><witsml:strengthForm uom="g/cm3">0</witsml:strengthForm><witsml:mdStrengthForm uom="m">0</witsml:mdStrengthForm><witsml:tvdStrengthForm uom="m">0</witsml:tvdStrengthForm><witsml:diaCsgLast uom="in">14</witsml:diaCsgLast><witsml:mdCsgLast uom="m">2593.44</witsml:mdCsgLast><witsml:tvdCsgLast uom="m">2080.1</witsml:tvdCsgLast><witsml:mdPlanned uom="m">-9999</witsml:mdPlanned><witsml:distDrill uom="m">0</witsml:distDrill><witsml:elevKelly uom="m">67.2</witsml:elevKelly><witsml:sum24Hr>POOH with 16&quot; x 17 1/2&quot; geopilot and XR reamer BHA on 6 5/8&quot; DP from 1195 m to surface. R/B same in derrick. N/D and repaired leak in annular preventer.</witsml:sum24Hr><witsml:forecast24Hr>Repair leak in annular preventer. N/U. Perform BOP test. M/U and RIH with 16&quot; x 17 1/2&quot; BHA. (status at 06:00 dependent on progress of annular repair)</witsml:forecast24Hr><witsml:ropCurrent uom="m/h">-9999</witsml:ropCurrent></witsml:statusInfo>
<witsml:fluid><witsml:type>Versatec</witsml:type><witsml:dTim>2011-10-03T16:00:00.000Z</witsml:dTim><witsml:md uom="m">1603</witsml:md><witsml:presBopRating uom="bar">345</witsml:presBopRating ><witsml:mudClass>oil based</witsml:mudClass><witsml:density uom="g/cm3">1.36</witsml:density><witsml:pv uom="mPa.s">33</witsml:pv><witsml:yp uom="Pa">12</witsml:yp></witsml:fluid>
<witsml:extendedReport dTim="2011-10-04T00:00:00.000Z">Depth: 0. Dimanteled annular preventer to inspect/replace seals on outer cylinder. Depth: 0. Unable to retrieve outer cylinder from annular preventer with 2 tonn. Discussed further action with Cameron onshore duty. Waited for Cameron representative to get required rest to discuss further action. Meanwhile cleaned area around BOP and drill floor for further operation.</witsml:extendedReport >
<witsml:activity><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T00:30:00.000Z</witsml:dTimEnd><witsml:md uom="m">1175</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- repair</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>equipment failure</witsml:stateDetailActivity><witsml:comments>Flow checked well. Pumped 5 m3 with 1,64 sg slug.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T00:30:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T02:45:00.000Z</witsml:dTimEnd><witsml:md uom="m">135</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- repair</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>equipment failure</witsml:stateDetailActivity><witsml:comments>POOH with 16&quot; x 17 1/2&quot; geopilot and XR reamer BHA on 6 5/8&quot; DP from 1195 m to 135 m . Avg. tripping speed 850 m/hr. Avg. slips to slips time 1,1 min. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T02:45:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T03:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">135</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- repair</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>equipment failure</witsml:stateDetailActivity><witsml:comments>Performed pre job meeting prior to B/O and racking BHA. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T03:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T04:15:00.000Z</witsml:dTimEnd><witsml:md uom="m">25</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- repair</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>equipment failure</witsml:stateDetailActivity><witsml:comments>B/O and racked back 16&quot; x 17 1/2&quot; Geopilot and XR reamer BHA</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T04:15:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T04:30:00.000Z</witsml:dTimEnd><witsml:md uom="m">25</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- repair</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>equipment failure</witsml:stateDetailActivity><witsml:comments>Downloaded memory data from MWD.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T04:30:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T05:15:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- repair</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>equipment failure</witsml:stateDetailActivity><witsml:comments>B/O and racked back 16&quot; x 17 1/2&quot; Geopilot and XR reamer BHA</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T05:15:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T06:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- maintain</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>equipment failure</witsml:stateDetailActivity><witsml:comments>Prepared for repairing annular preventer. Removed PS-30, diverter, mandrel etc.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T06:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T07:45:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>equipment failure</witsml:stateDetailActivity><witsml:comments>Performed pre job meeting with new crew prior to N/D diverter and mandrel. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T07:45:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T09:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- maintain</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>equipment failure</witsml:stateDetailActivity><witsml:comments>N/D diverter and mandrel. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T09:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T09:45:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- maintain</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>equipment failure</witsml:stateDetailActivity><witsml:comments>Cleaned annular preventer.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T09:45:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T10:30:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>equipment failure</witsml:stateDetailActivity><witsml:comments>Performed pre job meeting prior to repairing annular preventer. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T10:30:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- maintain</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>equipment failure</witsml:stateDetailActivity><witsml:comments>Repaired annular preventer. Removed top on annular preventer. Replaced seals. No visible damage on seals. Inspected annular element. No excessive damage to packer element. Dimanteled annular preventer to inspect/replace seals on outer cylinder.</witsml:comments></witsml:activity>
</witsml:drillReport></witsml:drillReports>
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<witsml:drillReports version="1.4.0.0" xmlns:witsml="http://www.witsml.org/schemas/1series" xmlns:xsi="http://www.w3.org/2001/XMLSchema-instance" xsi:schemaLocation="http://www.witsml.org/schemas/1series http://www.npd.no/schema//DDRS/1series/WITSML_drillReport_profiled_schema_phase2.xsd"><witsml:documentInfo><witsml:documentName>Drill Report</witsml:documentName><witsml:owner>IIP</witsml:owner></witsml:documentInfo><witsml:drillReport><witsml:nameWell>NO 31/2-D-2 AY3H</witsml:nameWell><witsml:nameWellbore>NO 31/2-D-2 AY3H</witsml:nameWellbore><witsml:name>name</witsml:name><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:versionKind>normal</witsml:versionKind><witsml:createDate>2011-10-05T07:56:31.000Z</witsml:createDate>
<witsml:wellAlias><witsml:name>31/2-D-2 AY3H</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellAlias>
<witsml:wellboreAlias><witsml:name>31/2-D-2 AY3H</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellboreAlias><witsml:wellboreAlias><witsml:name>6621</witsml:name><witsml:namingSystem>NPD number</witsml:namingSystem></witsml:wellboreAlias>
<witsml:wellboreInfo><witsml:operator>Statoil</witsml:operator><witsml:drillContractor>North Atlantic Drilling Limited </witsml:drillContractor><witsml:rigAlias><witsml:name>WEST VENTURE</witsml:name><witsml:namingSystem>NPD Name</witsml:namingSystem></witsml:rigAlias><witsml:rigAlias><witsml:name>297055</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:rigAlias></witsml:wellboreInfo>
<witsml:statusInfo><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">-9999</witsml:md><witsml:diaHole uom="in">0</witsml:diaHole><witsml:mdDiaHoleStart uom="m">1925</witsml:mdDiaHoleStart><witsml:strengthForm uom="g/cm3">1.4</witsml:strengthForm><witsml:mdStrengthForm uom="m">1566</witsml:mdStrengthForm><witsml:tvdStrengthForm uom="m">1482.2</witsml:tvdStrengthForm><witsml:diaCsgLast uom="in">9.625</witsml:diaCsgLast><witsml:mdCsgLast uom="m">1934.5</witsml:mdCsgLast><witsml:tvdCsgLast uom="m">1603.5</witsml:tvdCsgLast><witsml:presTestType>formation integrity test</witsml:presTestType><witsml:mdPlanned uom="m">-9999</witsml:mdPlanned><witsml:distDrill uom="m">-9999</witsml:distDrill><witsml:elevKelly uom="m">35.5</witsml:elevKelly><witsml:sum24Hr>Inflow tested DHSV.
Installed tubing hanger debris plug.
Disconnected and pulled THROT.
Prepared for pulling BOP.</witsml:sum24Hr><witsml:forecast24Hr>Waiting for a suitable weather window for pulling of BOP</witsml:forecast24Hr><witsml:ropCurrent uom="m/h">-9999</witsml:ropCurrent></witsml:statusInfo>
<witsml:fluid><witsml:type>NaCl Solids Free</witsml:type><witsml:dTim>2011-10-03T15:00:00.000Z</witsml:dTim><witsml:md uom="m">-9999</witsml:md><witsml:presBopRating uom="bar">1034</witsml:presBopRating ><witsml:mudClass>water based</witsml:mudClass><witsml:density uom="g/cm3">1.12</witsml:density><witsml:pv uom="mPa.s">13</witsml:pv><witsml:yp uom="Pa">7.5</witsml:yp></witsml:fluid>
<witsml:extendedReport dTim="2011-10-04T00:00:00.000Z">Depth: 0. further operations stopped as weather is too rough for pulling of BOP .
Estimated weather window for pulling of BOP is Oct. 5, afternoon and onwards.
Weather/ rig movements at 0600hrs :19 m/s, max waves 8,7 m, pitch 5,5 deg, roll 4,8 deg, heave 2,9 m
</witsml:extendedReport >
<witsml:activity><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T02:45:00.000Z</witsml:dTimEnd><witsml:md uom="m">1925</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>completion -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Inflow tested DHSV as follows: Pressured up string to 125 bar against both HCM-A&apos;s and GLV. Closed DHSV and bled off pressure above to 55 bar and monitored 1/2 hr for pressure build-up. Bled further to 5 bar and monitored 10 min for pressure build-up. Equalized pressure across DHSV w 125 bar and opened DHSV, then bled off pressure to zero. Confirmed total volume pumped in equalling total volume bled off. Closed DHSV. Final status : Both HCM-A&apos;s and GLV closed</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T02:45:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T04:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">1925</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>completion -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Rigged up wireline equipment and toolstring with 4.688&quot; R-line plug</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T04:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T05:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">371.2</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>completion -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Set 4,688&quot; debris plug in wellhead nipple profile.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T05:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T06:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">371.2</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>completion -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Pulled out with wireline toolstring and rigged down.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T06:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T10:45:00.000Z</witsml:dTimEnd><witsml:md uom="m">371.2</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>completion -- bop/wellhead equipment</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Retracted THROT indicator pin and unlatched THROT. Disconnected THROT and pulled above BOP.
Broke out XO-block and laid out same in chute and dismantled working platform and 2&quot; hose. Removed 16&quot; elevator and the extra long bails and installed 500 t drilling bails and elevator. Laid out lo-torque manifold and hoses prior to tripping.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T10:45:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T14:15:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>completion -- bop/wellhead equipment</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Pulled out with THROT and laid out same</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T14:15:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T15:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>plug abandon -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Cleaned and tidied rig floor. Doped pipe and removed Weatherford tong from drill floor</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T15:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T18:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>plug abandon -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Changed to 450 t elevator, checked saver sub and removed rotary table. Installed spider.
Meanwhile displaced riser to sea water, kill/choke lines to drill water through boost line.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T18:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- waiting on weather</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Stopped further operations as weather window for pulling of BOP was not available on forecast. Estimated weather window for pulling of BOP is Oct. 5, afternoon and onwards.
Weather at 2400hrs : 20 m/s, max waves 6,7 m, pitch 4deg, roll 4 deg, heave 1,8
Meanwhile performed bi-weekly pressure testing of choke manifold.
</witsml:comments></witsml:activity>
</witsml:drillReport></witsml:drillReports>
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<witsml:drillReports version="1.4.0.0" xmlns:witsml="http://www.witsml.org/schemas/1series" xmlns:xsi="http://www.w3.org/2001/XMLSchema-instance" xsi:schemaLocation="http://www.witsml.org/schemas/1series http://www.npd.no/schema//DDRS/1series/WITSML_drillReport_profiled_schema_phase2.xsd"><witsml:documentInfo><witsml:documentName>Drill Report</witsml:documentName><witsml:owner>IIP</witsml:owner></witsml:documentInfo><witsml:drillReport><witsml:nameWell>NO 33/9-A-37 C</witsml:nameWell><witsml:nameWellbore>NO 33/9-A-37 C</witsml:nameWellbore><witsml:name>name</witsml:name><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:versionKind>normal</witsml:versionKind><witsml:createDate>2011-10-05T07:59:10.000Z</witsml:createDate>
<witsml:wellAlias><witsml:name>33/9-A-37 C</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellAlias>
<witsml:wellboreAlias><witsml:name>33/9-A-37 C</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellboreAlias><witsml:wellboreAlias><witsml:name>6610</witsml:name><witsml:namingSystem>NPD number</witsml:namingSystem></witsml:wellboreAlias>
<witsml:wellboreInfo><witsml:dTimSpud>2011-06-01T00:00:00.000Z</witsml:dTimSpud><witsml:operator>Statoil</witsml:operator><witsml:drillContractor>Archer</witsml:drillContractor><witsml:rigAlias><witsml:name>STATFJORD A</witsml:name><witsml:namingSystem>NPD Name</witsml:namingSystem></witsml:rigAlias><witsml:rigAlias><witsml:name>271273</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:rigAlias></witsml:wellboreInfo>
<witsml:statusInfo><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">2497</witsml:md><witsml:tvd uom="m">2472.5</witsml:tvd><witsml:diaHole uom="in">8.5</witsml:diaHole><witsml:mdDiaHoleStart uom="m">2465</witsml:mdDiaHoleStart><witsml:strengthForm uom="g/cm3">1.62</witsml:strengthForm><witsml:mdStrengthForm uom="m">2463</witsml:mdStrengthForm><witsml:tvdStrengthForm uom="m">2440</witsml:tvdStrengthForm><witsml:diaCsgLast uom="in">9.625</witsml:diaCsgLast><witsml:mdCsgLast uom="m">2463.5</witsml:mdCsgLast><witsml:presTestType>formation integrity test</witsml:presTestType><witsml:mdPlanned uom="m">-9999</witsml:mdPlanned><witsml:distDrill uom="m">-9999</witsml:distDrill><witsml:elevKelly uom="m">64.5</witsml:elevKelly><witsml:sum24Hr>Waited for additional premix to arrive on location. Offloaded boat and started to mix new 1,23 sg WARP mud. Pulled out of hole to 1999 m. Draw-work disc brake failure caused elevator to land on rotary, setting down 20 tons. Troubleshot failed brake and loss of power to draw-works electric motors. Well was observed on trip tank while troubleshooting.</witsml:sum24Hr><witsml:forecast24Hr>Continue to troubleshoot and rectify fault in draw-work brake system. Continue to pull out of hole to 800 m and commence displacing well to 1,23 sg WARP mud in stages.</witsml:forecast24Hr><witsml:ropCurrent uom="m/h">-9999</witsml:ropCurrent></witsml:statusInfo>
<witsml:bitRecord><witsml:numBit>7</witsml:numBit><witsml:diaBit uom="in">8.5</witsml:diaBit><witsml:manufacturer>Security DBS</witsml:manufacturer><witsml:codeMfg>FMR3753Z</witsml:codeMfg></witsml:bitRecord>
<witsml:fluid><witsml:type>WARP (Oil Based)</witsml:type><witsml:dTim>2011-10-03T20:00:00.000Z</witsml:dTim><witsml:md uom="m">2497</witsml:md><witsml:presBopRating uom="bar">345</witsml:presBopRating ><witsml:mudClass>oil based</witsml:mudClass><witsml:density uom="g/cm3">1.23</witsml:density><witsml:pv uom="mPa.s">14</witsml:pv><witsml:yp uom="Pa">2</witsml:yp></witsml:fluid>
<witsml:porePressure><witsml:readingKind>estimated</witsml:readingKind><witsml:equivalentMudWeight uom="g/cm3">.98</witsml:equivalentMudWeight><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">2497</witsml:md></witsml:porePressure>
<witsml:extendedReport dTim="2011-10-04T00:00:00.000Z">Depth: 1999. Continued troubleshooting fault in draw-work control system. Observed well on trip tank. </witsml:extendedReport >
<witsml:activity><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T06:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">2444</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- wait</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited for additional amount of premix required for reduction of mudweight to arrive.
Continued to observe well and reciprocate drill string at intervalls to ensure free movement.
Performed planned maintenance while waiting.
</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T06:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T09:45:00.000Z</witsml:dTimEnd><witsml:md uom="m">2444</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- wait</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited for additional amount of premix required for reduction of mudweight to arrive.
Offloaded boat and started to mix new WARP mud with 1,23 sg.
Continued to observe well and reciprocate drill string at intervalls to ensure free movement.
Performed planned maintenance while waiting.
</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T09:45:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T11:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">1999</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>drilling -- trip</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Pulled out of hole from 2444 m to 1999 m (average pulling speed: 356 m/hr).
Operation stopped due to draw-work brake failure.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T11:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">1999</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- maintain</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>equipment failure</witsml:stateDetailActivity><witsml:comments>Draw-work power and brake failure.
Upon coming down with an empty block the draw-works parking brake failed to engage, simultaneously as the electric motors for the draw-work tripped out. This caused the traveling block to slide down until elevator landed on top of slips in rotary table setting down 20 tons on bails/elevator.
Immediately started to troubleshoot fault in draw-work control system. Observed well on trip tank. </witsml:comments></witsml:activity>
</witsml:drillReport></witsml:drillReports>
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<witsml:drillReports version="1.4.0.0" xmlns:witsml="http://www.witsml.org/schemas/1series" xmlns:xsi="http://www.w3.org/2001/XMLSchema-instance" xsi:schemaLocation="http://www.witsml.org/schemas/1series http://www.npd.no/schema//DDRS/1series/WITSML_drillReport_profiled_schema_phase2.xsd"><witsml:documentInfo><witsml:documentName>Drill Report</witsml:documentName><witsml:owner>IIP</witsml:owner></witsml:documentInfo><witsml:drillReport><witsml:nameWell>NO 33/9-E-1 H</witsml:nameWell><witsml:nameWellbore>NO 33/9-E-1 H</witsml:nameWellbore><witsml:name>name</witsml:name><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:versionKind>normal</witsml:versionKind><witsml:createDate>2011-10-05T08:00:02.000Z</witsml:createDate>
<witsml:wellAlias><witsml:name>33/9-E-1 H</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellAlias>
<witsml:wellboreAlias><witsml:name>33/9-E-1 H</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellboreAlias><witsml:wellboreAlias><witsml:name>2417</witsml:name><witsml:namingSystem>NPD number</witsml:namingSystem></witsml:wellboreAlias>
<witsml:wellboreInfo><witsml:dTimSpud>1996-03-13T00:00:00.000Z</witsml:dTimSpud><witsml:operator>Statoil</witsml:operator><witsml:drillContractor>DeepOcean</witsml:drillContractor><witsml:rigAlias><witsml:name>EDDA FAUNA</witsml:name><witsml:namingSystem>NPD Name</witsml:namingSystem></witsml:rigAlias><witsml:rigAlias><witsml:name>403711</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:rigAlias></witsml:wellboreInfo>
<witsml:statusInfo><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">-9999</witsml:md><witsml:diaHole uom="in">0</witsml:diaHole><witsml:mdDiaHoleStart uom="m">0</witsml:mdDiaHoleStart><witsml:diaCsgLast uom="in">9.625</witsml:diaCsgLast><witsml:mdCsgLast uom="m">3322.2</witsml:mdCsgLast><witsml:mdPlanned uom="m">-9999</witsml:mdPlanned><witsml:distDrill uom="m">-9999</witsml:distDrill><witsml:elevKelly uom="m">2</witsml:elevKelly><witsml:sum24Hr>None</witsml:sum24Hr><witsml:forecast24Hr>None</witsml:forecast24Hr><witsml:ropCurrent uom="m/h">-9999</witsml:ropCurrent></witsml:statusInfo>
<witsml:extendedReport dTim="2011-10-04T00:00:00.000Z">Depth: 265. Continued mobilizing equipment for Statfjord Nord E-1 H, E-4 H and Vigdis G-1 H.</witsml:extendedReport >
<witsml:activity><witsml:dTimStart>2011-10-03T12:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">262</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>workover -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Started mobilising equipment for well Statfjord E-1 H, E-4 H and Vigdis G-1 H.</witsml:comments></witsml:activity>
</witsml:drillReport></witsml:drillReports>
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<witsml:drillReports version="1.4.0.0" xmlns:witsml="http://www.witsml.org/schemas/1series" xmlns:xsi="http://www.w3.org/2001/XMLSchema-instance" xsi:schemaLocation="http://www.witsml.org/schemas/1series http://www.npd.no/schema//DDRS/1series/WITSML_drillReport_profiled_schema_phase2.xsd"><witsml:documentInfo><witsml:documentName>Drill Report</witsml:documentName><witsml:owner>IIP</witsml:owner></witsml:documentInfo><witsml:drillReport><witsml:nameWell>NO 33/9-M-3 H</witsml:nameWell><witsml:nameWellbore>NO 33/9-M-3 H</witsml:nameWellbore><witsml:name>name</witsml:name><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:versionKind>normal</witsml:versionKind><witsml:createDate>2011-10-05T08:00:24.000Z</witsml:createDate>
<witsml:wellAlias><witsml:name>33/9-M-3 H</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellAlias>
<witsml:wellboreAlias><witsml:name>33/9-M-3 H</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellboreAlias><witsml:wellboreAlias><witsml:name>4445</witsml:name><witsml:namingSystem>NPD number</witsml:namingSystem></witsml:wellboreAlias>
<witsml:wellboreInfo><witsml:dateDrillComplete>2002-01-14</witsml:dateDrillComplete><witsml:operator>Statoil</witsml:operator><witsml:drillContractor>Island Offshore Management</witsml:drillContractor><witsml:rigAlias><witsml:name>ISLAND FRONTIER</witsml:name><witsml:namingSystem>NPD Name</witsml:namingSystem></witsml:rigAlias><witsml:rigAlias><witsml:name>373829</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:rigAlias></witsml:wellboreInfo>
<witsml:statusInfo><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">-9999</witsml:md><witsml:diaHole uom="in">0</witsml:diaHole><witsml:mdDiaHoleStart uom="m">222</witsml:mdDiaHoleStart><witsml:diaCsgLast uom="in">5.5</witsml:diaCsgLast><witsml:mdCsgLast uom="m">4512.5</witsml:mdCsgLast><witsml:tvdCsgLast uom="m">2536</witsml:tvdCsgLast><witsml:presTestType>formation integrity test</witsml:presTestType><witsml:mdPlanned uom="m">-9999</witsml:mdPlanned><witsml:distDrill uom="m">-9999</witsml:distDrill><witsml:elevKelly uom="m">3</witsml:elevKelly><witsml:sum24Hr>Transit to shore, with stop at Fedjeosen for lubrication of ROV umbilical¿s. Moored alongside RO-RO quay at CCB. Demobilized Statfjord Øst M-3H equipment.</witsml:sum24Hr><witsml:forecast24Hr>Complete demobilizing Statfjord Øst M-3H equipment.
Status 06:00 No operation
</witsml:forecast24Hr><witsml:ropCurrent uom="m/h">-9999</witsml:ropCurrent></witsml:statusInfo>
<witsml:extendedReport dTim="2011-10-04T00:00:00.000Z">Depth: 0. </witsml:extendedReport >
<witsml:activity><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T02:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>workover -- bop/wellhead equipment</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Retrieved TCRT to surface. Released &amp; retrieved GW#3. Landed TCRT on skid and disconnected LS reel.Skid out TCRT and sea fastened same.
Meanwhile:
ROV closed ROV basket .
</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T02:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T04:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>workover -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Deployed GW#3 connect ROV hook on transponders and retrieved to surface. Deployed GW # 3 connect ROV hook on ROV basked and retrieved to surface.Performed valve status check. Opened 3-C Annulus manifold valve 90º CCW.
</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T04:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T05:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>workover -- bop/wellhead equipment</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Deployed GW #3 w/forerunner for close hatchers. Closed hatches. Retrieved GW #3.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T05:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T06:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>workover -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Performed as left survey. Opened MC 31 with 35 turn CCW and 237 NM. Retrieved Magnum ROV.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T06:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T14:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>moving -- transit</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Transit to shore, with stop at Fedjeosen for lubrication of ROV umbilicals. ETA 19:00 CCB. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T14:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T16:30:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>moving -- transit</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Deployed both ROV&apos;s and lubricated the umbilicals.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T16:30:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T19:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>moving -- transit</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Continued transit to shore, ETA 19:00 CCB. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T19:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>workover -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Moored alongside RO-RO quay at CCB. Skid stack into MTH. Split stack and skid out connector.
Cut off sea fasting on deck.
Backloaded:
AWS / Halliburton Explosive cont.
Welltec 8m basked
2 ea AWS 7/16 logging cont.
Halliburton 8m basked.
Baker oil tool basked.
Halliburton 8 ft container.
Connector.</witsml:comments></witsml:activity>
</witsml:drillReport></witsml:drillReports>
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<witsml:drillReports version="1.4.0.0" xmlns:witsml="http://www.witsml.org/schemas/1series" xmlns:xsi="http://www.w3.org/2001/XMLSchema-instance" xsi:schemaLocation="http://www.witsml.org/schemas/1series http://www.npd.no/schema//DDRS/1series/WITSML_drillReport_profiled_schema_phase2.xsd"><witsml:documentInfo><witsml:documentName>Drill Report</witsml:documentName><witsml:owner>IIP</witsml:owner></witsml:documentInfo><witsml:drillReport><witsml:nameWell>NO 34/10-A-35</witsml:nameWell><witsml:nameWellbore>NO 34/10-A-35</witsml:nameWellbore><witsml:name>name</witsml:name><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:versionKind>normal</witsml:versionKind><witsml:createDate>2011-10-05T08:03:18.000Z</witsml:createDate>
<witsml:wellAlias><witsml:name>34/10-A-35</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellAlias>
<witsml:wellboreAlias><witsml:name>34/10-A-35</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellboreAlias><witsml:wellboreAlias><witsml:name>1876</witsml:name><witsml:namingSystem>NPD number</witsml:namingSystem></witsml:wellboreAlias>
<witsml:wellboreInfo><witsml:dTimSpud>1992-01-27T00:00:00.000Z</witsml:dTimSpud><witsml:operator>Statoil</witsml:operator><witsml:drillContractor>Halliburton</witsml:drillContractor><witsml:rigAlias><witsml:name>GULLFAKS A</witsml:name><witsml:namingSystem>NPD Name</witsml:namingSystem></witsml:rigAlias><witsml:rigAlias><witsml:name>271833</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:rigAlias></witsml:wellboreInfo>
<witsml:statusInfo><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">-9999</witsml:md><witsml:diaHole uom="in">0</witsml:diaHole><witsml:diaCsgLast uom="in">5</witsml:diaCsgLast><witsml:mdCsgLast uom="m">3017</witsml:mdCsgLast><witsml:mdPlanned uom="m">-9999</witsml:mdPlanned><witsml:distDrill uom="m">-9999</witsml:distDrill><witsml:elevKelly uom="m">85</witsml:elevKelly><witsml:sum24Hr>Waited for boat to return to platform with fourth batch of silicate solution. Boat waiting to load on Batch#4 due to bad weather.</witsml:sum24Hr><witsml:forecast24Hr> Waiting for chemicals to arrive from shore. </witsml:forecast24Hr><witsml:ropCurrent uom="m/h">-9999</witsml:ropCurrent></witsml:statusInfo>
<witsml:extendedReport dTim="2011-10-04T00:00:00.000Z">Depth: 0. Waited for boat to return to platform with fourth batch of silicate solution. Boat waiting to load on Batch#4 due to bad weather.</witsml:extendedReport >
<witsml:activity><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T06:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- waiting on weather</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited for boat to return to platform with fourth batch of silicate solution. Boat waiting to load on Batch#4 due to bad weather.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T06:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- waiting on weather</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited for boat to return to platform with fourth batch of silicate solution. Boat waiting to load on Batch#4 due to bad weather.</witsml:comments></witsml:activity>
</witsml:drillReport></witsml:drillReports>
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<witsml:drillReports version="1.4.0.0" xmlns:witsml="http://www.witsml.org/schemas/1series" xmlns:xsi="http://www.w3.org/2001/XMLSchema-instance" xsi:schemaLocation="http://www.witsml.org/schemas/1series http://www.npd.no/schema//DDRS/1series/WITSML_drillReport_profiled_schema_phase2.xsd"><witsml:documentInfo><witsml:documentName>Drill Report</witsml:documentName><witsml:owner>IIP</witsml:owner></witsml:documentInfo><witsml:drillReport><witsml:nameWell>NO 34/10-A-40</witsml:nameWell><witsml:nameWellbore>NO 34/10-A-40</witsml:nameWellbore><witsml:name>name</witsml:name><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:versionKind>normal</witsml:versionKind><witsml:createDate>2011-10-05T08:03:40.000Z</witsml:createDate>
<witsml:wellAlias><witsml:name>34/10-A-40</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellAlias>
<witsml:wellboreAlias><witsml:name>34/10-A-40</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellboreAlias><witsml:wellboreAlias><witsml:name>2070</witsml:name><witsml:namingSystem>NPD number</witsml:namingSystem></witsml:wellboreAlias>
<witsml:wellboreInfo><witsml:dTimSpud>1993-04-30T00:00:00.000Z</witsml:dTimSpud><witsml:operator>Statoil</witsml:operator><witsml:drillContractor>Aker Solution Services</witsml:drillContractor><witsml:rigAlias><witsml:name>GULLFAKS A</witsml:name><witsml:namingSystem>NPD Name</witsml:namingSystem></witsml:rigAlias><witsml:rigAlias><witsml:name>271833</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:rigAlias></witsml:wellboreInfo>
<witsml:statusInfo><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">-9999</witsml:md><witsml:diaHole uom="in">0</witsml:diaHole><witsml:mdDiaHoleStart uom="m">547</witsml:mdDiaHoleStart><witsml:diaCsgLast uom="in">5</witsml:diaCsgLast><witsml:mdCsgLast uom="m">4949</witsml:mdCsgLast><witsml:tvdCsgLast uom="m">1860</witsml:tvdCsgLast><witsml:mdPlanned uom="m">-9999</witsml:mdPlanned><witsml:distDrill uom="m">-9999</witsml:distDrill><witsml:elevKelly uom="m">82</witsml:elevKelly><witsml:sum24Hr>Waited for logging operation in well A-10. RIH with BHA# 1 Tractor and RST to 475 m. WL cabin and grease Skid shutt down. POOH fom 475 m. Statoil fire &amp; gas tested and solved system for EL. WL equipment.</witsml:sum24Hr><witsml:forecast24Hr>RIH with BHA# 1 Tractor and RST. Log RST - D in Brent: 4340 - 3840 m and in Cook: 3720 - 3380 m. </witsml:forecast24Hr><witsml:ropCurrent uom="m/h">-9999</witsml:ropCurrent></witsml:statusInfo>
<witsml:extendedReport dTim="2011-10-04T00:00:00.000Z">Depth: 0. Equalized and opened HMV. Tested tractor and RST tool. Opened SV. WHP 92 bar. Depth: 2235. Ran in hole by gravity at 30 m/min lost weight at 2235 m. PU 50 m every 400 m (AWS procedure for new cable) Depth: 4280. Activated tractor and RIH from 2235 m to 4000 m 06:00. PU 50 m every 400 m (AWS procedure for new cable). Had to make 3 attempts to pass through straddle at 3548,5 m.</witsml:extendedReport >
<witsml:activity><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T06:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- wait</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited for logging operation in well A-10 to be completed. Common Slb acquisition computer. Meanwhile held A - standard / pre-job meeting with involved personnel on night shift.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T06:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T08:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- wait</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited for logging operation in well A-10 to be completed. Common Slb acquisition computer.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T08:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T09:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Performed A - standard / pre-job meeting with involved personnel on day shift.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T09:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T13:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- wait</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited for logging operation in well A-10 to be completed. Common Slb acquisition computer.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T13:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T15:45:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- wait</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited for logging operation in well A-10 to be completed. Common Slb acquisition computer.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T15:45:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T16:45:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Performed communication checks on logging tools. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T16:45:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T18:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Leaktested lubricator to 20/345 bar for 5/10 min with 100 % MEG. Opened HMV. WHP 93,8 bar. Pumped 50 ltr 100% MEG to equalize DHSV. Pumped 4 m3 of base oil. Openes swab. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T18:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T19:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Ran in hole by gravity at 30 m/min to 475 m. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T19:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T19:35:00.000Z</witsml:dTimEnd><witsml:md uom="m">475</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Winch cabin and unit for grease supply shut down. Loosed electric power due to gas alarm in D-21. AWS contacted SKR. Pressured up stuffing box to keep well control.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T19:45:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T20:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Gas alarm in D-21 cleared out. Electric power turned on. POOH from 475 m to surface. Closed SV and HMV.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T20:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T22:30:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Evaluated situation. Discussed situation w/ Statoil fire &amp; gas prod dep. and electrician for sorting out why override of ignitionsource disconnection system failed.
</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T22:30:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Statoil fire &amp; gas tested system for electric WL equipment. Solved the reason for cabin and grease loosed electric power shut down .Override of ignitionsource disconnection system for WL cabin was not activated on switchboard 17 - EN01.</witsml:comments></witsml:activity>
</witsml:drillReport></witsml:drillReports>
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<witsml:drillReports version="1.4.0.0" xmlns:witsml="http://www.witsml.org/schemas/1series" xmlns:xsi="http://www.w3.org/2001/XMLSchema-instance" xsi:schemaLocation="http://www.witsml.org/schemas/1series http://www.npd.no/schema//DDRS/1series/WITSML_drillReport_profiled_schema_phase2.xsd"><witsml:documentInfo><witsml:documentName>Drill Report</witsml:documentName><witsml:owner>IIP</witsml:owner></witsml:documentInfo><witsml:drillReport><witsml:nameWell>NO 34/10-B-40 A</witsml:nameWell><witsml:nameWellbore>NO 34/10-B-40 A</witsml:nameWellbore><witsml:name>name</witsml:name><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:versionKind>normal</witsml:versionKind><witsml:createDate>2011-10-05T08:04:03.000Z</witsml:createDate>
<witsml:wellAlias><witsml:name>34/10-B-40 A</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellAlias>
<witsml:wellboreAlias><witsml:name>34/10-B-40 A</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellboreAlias><witsml:wellboreAlias><witsml:name>3628</witsml:name><witsml:namingSystem>NPD number</witsml:namingSystem></witsml:wellboreAlias>
<witsml:wellboreInfo><witsml:operator>Statoil</witsml:operator><witsml:drillContractor>Aker Kvaerner Well Services</witsml:drillContractor><witsml:rigAlias><witsml:name>GULLFAKS B</witsml:name><witsml:namingSystem>NPD Name</witsml:namingSystem></witsml:rigAlias><witsml:rigAlias><witsml:name>271917</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:rigAlias></witsml:wellboreInfo>
<witsml:statusInfo><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">-9999</witsml:md><witsml:diaHole uom="in">0</witsml:diaHole><witsml:mdDiaHoleStart uom="m">4626</witsml:mdDiaHoleStart><witsml:diaCsgLast uom="in">4.5</witsml:diaCsgLast><witsml:mdCsgLast uom="m">4773</witsml:mdCsgLast><witsml:tvdCsgLast uom="m">2277.5</witsml:tvdCsgLast><witsml:presTestType>formation integrity test</witsml:presTestType><witsml:mdPlanned uom="m">-9999</witsml:mdPlanned><witsml:distDrill uom="m">-9999</witsml:distDrill><witsml:elevKelly uom="m">80.7</witsml:elevKelly><witsml:sum24Hr>Spotted equipment on BOP deck. Took over the well from production department. RU WL and pumping equipment on the well. On standby to lift up lubricator due to wind speed exceeded operation limit for WL crane. </witsml:sum24Hr><witsml:forecast24Hr>RIH with BHA#1 (WL brush). Spot Safe-Solv 148 and brush DHSV area. Inflow test DHSV and RD equipment from the well.</witsml:forecast24Hr><witsml:ropCurrent uom="m/h">-9999</witsml:ropCurrent></witsml:statusInfo>
<witsml:extendedReport dTim="2011-10-04T00:00:00.000Z">Depth: 0. Performed pre-job meeting with night crew. Depth: 0. Waited on weather. Continued on standby due to strong wind. Depth: 0. Function test Well Equip jar. MU BHA#1 (6,3&quot; brush with 6,1&quot; no-go) and installed in lubricator. Leak tested RU to 20/345 bar 5/10 min. </witsml:extendedReport >
<witsml:activity><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T00:30:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Performed startup meeting with night crew.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T00:30:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T06:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Spotted WL and pumping equipment on work area. Prepared brush BHA. Lined up pumping lines towards the well.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T06:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T09:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Cont. spotting equipment in BOP area. Built scaffolding around X-mas tree.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T09:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T12:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- wait</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited for activity program to be signed. Meanwhile had start up meeting with day crew.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T12:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T16:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- wait</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited for Production to hand over well.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T16:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T16:45:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Handed well over from Production to Well operation. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T16:45:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T21:15:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>RU pumping line from cement unit to KWV. RU lower riser and WL BOP. Function tested WL BOP. Leak tested riser and WL BOP to 20/345 bar for 5/10 mins. Leak tested pump line to 20/345 bar for 5/10 mins.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T21:15:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- waiting on weather</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Performed A-standard meeting, evaluated situation prior proceed operation with respect to strong wind. Secured work place. On standby to lift up lubricator and BHA due to wind speed was up to 58 knots while max allowable wind speed to operate WL crane is 48 knots according to APOS.</witsml:comments></witsml:activity>
</witsml:drillReport></witsml:drillReports>
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<witsml:drillReports version="1.4.0.0" xmlns:witsml="http://www.witsml.org/schemas/1series" xmlns:xsi="http://www.w3.org/2001/XMLSchema-instance" xsi:schemaLocation="http://www.witsml.org/schemas/1series http://www.npd.no/schema//DDRS/1series/WITSML_drillReport_profiled_schema_phase2.xsd"><witsml:documentInfo><witsml:documentName>Drill Report</witsml:documentName><witsml:owner>IIP</witsml:owner></witsml:documentInfo><witsml:drillReport><witsml:nameWell>NO 34/11-A-11</witsml:nameWell><witsml:nameWellbore>NO 34/11-A-11</witsml:nameWellbore><witsml:name>name</witsml:name><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:versionKind>normal</witsml:versionKind><witsml:createDate>2011-10-05T08:05:05.000Z</witsml:createDate>
<witsml:wellAlias><witsml:name>34/11-A-11</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellAlias>
<witsml:wellboreAlias><witsml:name>34/11-A-11</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellboreAlias><witsml:wellboreAlias><witsml:name>5001</witsml:name><witsml:namingSystem>NPD number</witsml:namingSystem></witsml:wellboreAlias>
<witsml:wellboreInfo><witsml:dateDrillComplete>2004-12-27</witsml:dateDrillComplete><witsml:operator>Statoil</witsml:operator><witsml:drillContractor>Aker Well Service</witsml:drillContractor><witsml:rigAlias><witsml:name>KVITEBJØRN</witsml:name><witsml:namingSystem>NPD Name</witsml:namingSystem></witsml:rigAlias><witsml:rigAlias><witsml:name>280877</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:rigAlias></witsml:wellboreInfo>
<witsml:statusInfo><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">-9999</witsml:md><witsml:diaHole uom="in">0</witsml:diaHole><witsml:mdDiaHoleStart uom="m">4389</witsml:mdDiaHoleStart><witsml:strengthForm uom="g/cm3">2.1</witsml:strengthForm><witsml:mdStrengthForm uom="m">4200</witsml:mdStrengthForm><witsml:tvdStrengthForm uom="m">3989</witsml:tvdStrengthForm><witsml:diaCsgLast uom="in">7</witsml:diaCsgLast><witsml:mdCsgLast uom="m">4483.2</witsml:mdCsgLast><witsml:presTestType>formation integrity test</witsml:presTestType><witsml:mdPlanned uom="m">-9999</witsml:mdPlanned><witsml:distDrill uom="m">-9999</witsml:distDrill><witsml:elevKelly uom="m">60.5</witsml:elevKelly><witsml:sum24Hr>Received logging equipment from town. Waited for Baker logging personnel to arrive. Baker personnel arrived. Handed well from Prod dept. to D&amp;W. Transferred controll of DHSV and HMV from platform system to local panel. Waited for Prod dept. to close in wells prior to performing critical lift</witsml:sum24Hr><witsml:forecast24Hr>Perform critical lift and rig on well. Prepare Baker logging equipment. MU BHA no 1 with CMI logging tool. RIH with CMI logging tool to TD. Logg with CMI tool according to program.</witsml:forecast24Hr><witsml:ropCurrent uom="m/h">-9999</witsml:ropCurrent></witsml:statusInfo>
<witsml:fluid><witsml:type>Fresh Water</witsml:type><witsml:dTim>2011-10-03T16:00:00.000Z</witsml:dTim><witsml:md uom="m">-9999</witsml:md><witsml:presBopRating uom="bar">827</witsml:presBopRating ><witsml:mudClass>water based</witsml:mudClass><witsml:density uom="g/cm3">1.05</witsml:density><witsml:pv uom="mPa.s">-9999</witsml:pv><witsml:yp uom="Pa">-9999</witsml:yp></witsml:fluid>
<witsml:extendedReport dTim="2011-10-04T00:00:00.000Z">Depth: 0. Disconnected KWV end cap and RU kill line to KWV. Meanwhile Production department to close in wells prior to performing critical lift. Depth: 0. Changed hatch cover to WL hatch. Removed X-mas top cap. Performed critical lift and landed wireline stack onto x-mas tree. MU clamp on lower riser. Depth: 0. Function tested BOP Depth: 0. Leak tested with cmt unit against closed Lo-Tq valve outside KVW to 20/ 445 bar for 5/ 10 min Depth: 0. Leak tested against closed KWV to 20/ 445 bar for 5/ 10 min.</witsml:extendedReport >
<witsml:activity><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T01:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Received logging equipment from town. Spotted tool containers and logging cabin on pipedeck.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T01:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T06:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited for Baker logging personnel to arrive. Meanwhile held A-standard training with topic leak testing and prepared equipment for 5/16&quot; mono cable operation.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T06:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T18:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- wait</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited for Baker logging personnel to arrive. Meanwhile prepared WL equipment.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T18:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T20:30:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Baker personnel arrived. New arrived Baker personnel on platform introduction brief.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T20:30:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T21:15:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Performed pre job meeting with involved personnel.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T21:15:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T22:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Handed well from Prod dept. to D&amp;W. Transferred controll of DHSV and HMV from platform system to local panel. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T22:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T22:45:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Preformed SJA and DOP meeting prior critical lifting operations (RU WL riser incl WL BOP).</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T22:45:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- wait</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited for Production department to close in wells prior to performing critical lift.</witsml:comments></witsml:activity>
</witsml:drillReport></witsml:drillReports>
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<witsml:drillReports version="1.4.0.0" xmlns:witsml="http://www.witsml.org/schemas/1series" xmlns:xsi="http://www.w3.org/2001/XMLSchema-instance" xsi:schemaLocation="http://www.witsml.org/schemas/1series http://www.npd.no/schema//DDRS/1series/WITSML_drillReport_profiled_schema_phase2.xsd"><witsml:documentInfo><witsml:documentName>Drill Report</witsml:documentName><witsml:owner>IIP</witsml:owner></witsml:documentInfo><witsml:drillReport><witsml:nameWell>NO 34/4-C-8 H</witsml:nameWell><witsml:nameWellbore>NO 34/4-C-8 H</witsml:nameWellbore><witsml:name>name</witsml:name><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:versionKind>normal</witsml:versionKind><witsml:createDate>2011-10-05T08:01:15.000Z</witsml:createDate>
<witsml:wellAlias><witsml:name>34/4-C-8 H</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellAlias>
<witsml:wellboreAlias><witsml:name>34/4-C-8 H</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellboreAlias><witsml:wellboreAlias><witsml:name>6546</witsml:name><witsml:namingSystem>NPD number</witsml:namingSystem></witsml:wellboreAlias>
<witsml:wellboreInfo><witsml:dTimSpud>2005-06-02T00:00:00.000Z</witsml:dTimSpud><witsml:dateDrillComplete>2011-07-05</witsml:dateDrillComplete><witsml:operator>Statoil</witsml:operator><witsml:drillContractor>Odfjell Drilling AS</witsml:drillContractor><witsml:rigAlias><witsml:name>SNORRE B</witsml:name><witsml:namingSystem>NPD Name</witsml:namingSystem></witsml:rigAlias><witsml:rigAlias><witsml:name>280485</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:rigAlias></witsml:wellboreInfo>
<witsml:statusInfo><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">0</witsml:md><witsml:tvd uom="m">0</witsml:tvd><witsml:diaHole uom="in">0</witsml:diaHole><witsml:mdDiaHoleStart uom="m">4427.6</witsml:mdDiaHoleStart><witsml:strengthForm uom="g/cm3">1.69</witsml:strengthForm><witsml:mdStrengthForm uom="m">3944</witsml:mdStrengthForm><witsml:tvdStrengthForm uom="m">2472</witsml:tvdStrengthForm><witsml:diaCsgLast uom="in">7</witsml:diaCsgLast><witsml:mdCsgLast uom="m">4641.7</witsml:mdCsgLast><witsml:tvdCsgLast uom="m">2637</witsml:tvdCsgLast><witsml:presTestType>formation integrity test</witsml:presTestType><witsml:mdPlanned uom="m">-9999</witsml:mdPlanned><witsml:distDrill uom="m">-9999</witsml:distDrill><witsml:elevKelly uom="m">37</witsml:elevKelly><witsml:sum24Hr>Waited for 60 hrs weather window to run completion string to production packer.</witsml:sum24Hr><witsml:forecast24Hr>Wait for weather window to run completion string to production packer.</witsml:forecast24Hr><witsml:ropCurrent uom="m/h">-9999</witsml:ropCurrent></witsml:statusInfo>
<witsml:fluid><witsml:type>Cs/KFormate </witsml:type><witsml:dTim>2011-10-03T15:00:00.000Z</witsml:dTim><witsml:md uom="m">4645</witsml:md><witsml:presBopRating uom="bar">345</witsml:presBopRating ><witsml:mudClass>water based</witsml:mudClass><witsml:density uom="g/cm3">1.63</witsml:density><witsml:pv uom="mPa.s">26</witsml:pv><witsml:yp uom="Pa">14</witsml:yp></witsml:fluid>
<witsml:extendedReport dTim="2011-10-04T00:00:00.000Z">Depth: 0. Waited for 60 hrs weather window to run completion string to production packer.
Max heave observed 6,8 m.
Meanwhile performed general maintenance on drilling equipment.</witsml:extendedReport >
<witsml:activity><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T06:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- waiting on weather</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited for 60 hrs weather window to be able to RIH with comletion string to prod.packer.
Meanwhile performed general maintenance on drilling equipment. Broke down drill pipe stand. Washed and greased threads, racked back same.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T06:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- waiting on weather</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited for 60 hrs weather window to be able to RIH with comletion string to prod.packer.
Meanwhile performed general maintenance on drilling equipment.</witsml:comments></witsml:activity>
</witsml:drillReport></witsml:drillReports>
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<witsml:drillReports version="1.4.0.0" xmlns:witsml="http://www.witsml.org/schemas/1series" xmlns:xsi="http://www.w3.org/2001/XMLSchema-instance" xsi:schemaLocation="http://www.witsml.org/schemas/1series http://www.npd.no/schema//DDRS/1series/WITSML_drillReport_profiled_schema_phase2.xsd"><witsml:documentInfo><witsml:documentName>Drill Report</witsml:documentName><witsml:owner>IIP</witsml:owner></witsml:documentInfo><witsml:drillReport><witsml:nameWell>NO 34/7-C-2 AH</witsml:nameWell><witsml:nameWellbore>NO 34/7-C-2 AHT4</witsml:nameWellbore><witsml:name>name</witsml:name><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:versionKind>normal</witsml:versionKind><witsml:createDate>2011-10-05T08:01:43.000Z</witsml:createDate>
<witsml:wellAlias><witsml:name>34/7-C-2 AH</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellAlias>
<witsml:wellboreAlias><witsml:name>34/7-C-2 AHT4</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellboreAlias><witsml:wellboreAlias><witsml:name>4341</witsml:name><witsml:namingSystem>NPD number</witsml:namingSystem></witsml:wellboreAlias>
<witsml:wellboreInfo><witsml:dTimSpud>2001-09-21T00:00:00.000Z</witsml:dTimSpud><witsml:operator>Statoil</witsml:operator><witsml:drillContractor>Island Offshore Management</witsml:drillContractor><witsml:rigAlias><witsml:name>ISLAND FRONTIER</witsml:name><witsml:namingSystem>NPD Name</witsml:namingSystem></witsml:rigAlias><witsml:rigAlias><witsml:name>373829</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:rigAlias></witsml:wellboreInfo>
<witsml:statusInfo><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">-9999</witsml:md><witsml:diaHole uom="in">0</witsml:diaHole><witsml:mdDiaHoleStart uom="m">4660</witsml:mdDiaHoleStart><witsml:mdKickoff uom="m">3177</witsml:mdKickoff><witsml:diaCsgLast uom="in">5.5</witsml:diaCsgLast><witsml:mdCsgLast uom="m">4629</witsml:mdCsgLast><witsml:mdPlanned uom="m">-9999</witsml:mdPlanned><witsml:distDrill uom="m">-9999</witsml:distDrill><witsml:elevKelly uom="m">2</witsml:elevKelly><witsml:sum24Hr>None</witsml:sum24Hr><witsml:forecast24Hr>None</witsml:forecast24Hr><witsml:ropCurrent uom="m/h">-9999</witsml:ropCurrent></witsml:statusInfo>
<witsml:extendedReport dTim="2011-10-04T00:00:00.000Z">Depth: 0. Lifted onboard Vetco connector. Connected stack to connector. Performed between well check on stack.
Took onboard: AWS plug container.
Back loaded: TCRT, Pariser wheel., 3 ea pop-off valve to be re-set, 2 ea HW 443 tand, 1 CPI work container, 1 ea 6m guide post.</witsml:extendedReport >
</witsml:drillReport></witsml:drillReports>
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<witsml:drillReports version="1.4.0.0" xmlns:witsml="http://www.witsml.org/schemas/1series" xmlns:xsi="http://www.w3.org/2001/XMLSchema-instance" xsi:schemaLocation="http://www.witsml.org/schemas/1series http://www.npd.no/schema//DDRS/1series/WITSML_drillReport_profiled_schema_phase2.xsd"><witsml:documentInfo><witsml:documentName>Drill Report</witsml:documentName><witsml:owner>IIP</witsml:owner></witsml:documentInfo><witsml:drillReport><witsml:nameWell>NO 34/7-P-7</witsml:nameWell><witsml:nameWellbore>NO 34/7-P-7</witsml:nameWellbore><witsml:name>name</witsml:name><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:versionKind>normal</witsml:versionKind><witsml:createDate>2011-10-05T08:02:11.000Z</witsml:createDate>
<witsml:wellAlias><witsml:name>34/7-P-7</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellAlias>
<witsml:wellboreAlias><witsml:name>34/7-P-7</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellboreAlias><witsml:wellboreAlias><witsml:name>1720</witsml:name><witsml:namingSystem>NPD number</witsml:namingSystem></witsml:wellboreAlias>
<witsml:wellboreInfo><witsml:dTimSpud>1991-07-14T00:00:00.000Z</witsml:dTimSpud><witsml:operator>Statoil</witsml:operator><witsml:drillContractor>BJ Services</witsml:drillContractor><witsml:rigAlias><witsml:name>SNORRE A</witsml:name><witsml:namingSystem>NPD Name</witsml:namingSystem></witsml:rigAlias><witsml:rigAlias><witsml:name>272085</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:rigAlias></witsml:wellboreInfo>
<witsml:statusInfo><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">-9999</witsml:md><witsml:diaHole uom="in">0</witsml:diaHole><witsml:mdDiaHoleStart uom="m">0</witsml:mdDiaHoleStart><witsml:mdKickoff uom="m">368.4</witsml:mdKickoff><witsml:strengthForm uom="g/cm3">0</witsml:strengthForm><witsml:mdStrengthForm uom="m">0</witsml:mdStrengthForm><witsml:tvdStrengthForm uom="m">0</witsml:tvdStrengthForm><witsml:diaCsgLast uom="in">5.5</witsml:diaCsgLast><witsml:mdCsgLast uom="m">4779.6</witsml:mdCsgLast><witsml:mdPlanned uom="m">-9999</witsml:mdPlanned><witsml:distDrill uom="m">-9999</witsml:distDrill><witsml:elevKelly uom="m">59.4</witsml:elevKelly><witsml:sum24Hr>Started to spot and prepare CT equipment prior to rig up. WOW.</witsml:sum24Hr><witsml:forecast24Hr>Continue to spot and prepare CT equipment prior to rig up.</witsml:forecast24Hr><witsml:ropCurrent uom="m/h">-9999</witsml:ropCurrent></witsml:statusInfo>
<witsml:extendedReport dTim="2011-10-04T00:00:00.000Z">Depth: 0. WOW.</witsml:extendedReport >
<witsml:activity><witsml:dTimStart>2011-10-03T02:15:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T03:45:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>coil</witsml:phase><witsml:proprietaryCode>workover -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>All coiled tubing equipment onboard. Prepared rig crane prior to lifting CT reels.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T03:45:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T04:55:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>coil</witsml:phase><witsml:proprietaryCode>workover -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Repositioned CT reels. Lifted track and trolly to pipe deck and spotted same in position against well. Lifted power pack to pipe deck. Positioned turn table onto track and trolly. Positioned reel foundation onto turn table.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T04:55:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T06:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>coil</witsml:phase><witsml:proprietaryCode>workover -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Crane dep. busy with other crane operations. Meanwhile unpacked CT equipment.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T06:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T07:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>coil</witsml:phase><witsml:proprietaryCode>workover -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Looked for and found beams to put under the tool container. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T07:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T08:10:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>coil</witsml:phase><witsml:proprietaryCode>workover -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Activated work permit for working on pipe deck. Prepared rig up plan. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T08:10:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T09:05:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>coil</witsml:phase><witsml:proprietaryCode>interruption -- wait</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited due to crane lifting in pipe deck area.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T09:05:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T09:55:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>coil</witsml:phase><witsml:proprietaryCode>interruption -- wait</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited on electrician due to busy with other work.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T09:55:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T11:15:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>coil</witsml:phase><witsml:proprietaryCode>workover -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Hooked up CT power pack to platform fire &amp; gas system. Function tested CT power pack.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T11:15:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T12:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>coil</witsml:phase><witsml:proprietaryCode>workover -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Lifted 3 ea. beams for tool container up to pipe deck. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T12:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T13:30:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>coil</witsml:phase><witsml:proprietaryCode>interruption -- wait</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited on crane dep.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T13:30:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T15:15:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>coil</witsml:phase><witsml:proprietaryCode>workover -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Held tool box talk. Lifted CT reel into foundation and removed the bridle.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T15:15:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T17:10:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>coil</witsml:phase><witsml:proprietaryCode>interruption -- waiting on weather</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>WOW. To strong wind for crane operation.
Meanwhile started to disconnect power pack prior to replacing.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T17:10:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T17:50:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>coil</witsml:phase><witsml:proprietaryCode>workover -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Crane available. Repositioned CT reel cradle and foundation bridle. Lifted and positioned tool container onto beams.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T17:50:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>coil</witsml:phase><witsml:proprietaryCode>interruption -- waiting on weather</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>WOW.
Meanwhile:
Disconnected and prepared power pack prior to repositioning, due to drilling dep. needed more space on pipe deck.
Storm secured all CT equipment.
Held startup meeting for night shift crew.</witsml:comments></witsml:activity>
</witsml:drillReport></witsml:drillReports>
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<witsml:drillReports version="1.4.0.0" xmlns:witsml="http://www.witsml.org/schemas/1series" xmlns:xsi="http://www.w3.org/2001/XMLSchema-instance" xsi:schemaLocation="http://www.witsml.org/schemas/1series http://www.npd.no/schema//DDRS/1series/WITSML_drillReport_profiled_schema_phase2.xsd"><witsml:documentInfo><witsml:documentName>Drill Report</witsml:documentName><witsml:owner>IIP</witsml:owner></witsml:documentInfo><witsml:drillReport><witsml:nameWell>NO 35/8-Q-14 H</witsml:nameWell><witsml:nameWellbore>NO 35/8-Q-14 H</witsml:nameWellbore><witsml:name>name</witsml:name><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:versionKind>normal</witsml:versionKind><witsml:createDate>2011-10-05T08:05:25.000Z</witsml:createDate>
<witsml:wellAlias><witsml:name>35/8-Q-14 H</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellAlias>
<witsml:wellboreAlias><witsml:name>35/8-Q-14 H</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellboreAlias><witsml:wellboreAlias><witsml:name>6435</witsml:name><witsml:namingSystem>NPD number</witsml:namingSystem></witsml:wellboreAlias>
<witsml:wellboreInfo><witsml:dTimSpud>2010-08-14T00:00:00.000Z</witsml:dTimSpud><witsml:operator>Statoil</witsml:operator><witsml:drillContractor>Dolphin</witsml:drillContractor><witsml:rigAlias><witsml:name>BIDEFORD DOLPHIN</witsml:name><witsml:namingSystem>NPD Name</witsml:namingSystem></witsml:rigAlias><witsml:rigAlias><witsml:name>290170</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:rigAlias></witsml:wellboreInfo>
<witsml:statusInfo><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">4751</witsml:md><witsml:tvd uom="m">3649</witsml:tvd><witsml:diaHole uom="in">0</witsml:diaHole><witsml:strengthForm uom="g/cm3">1.95</witsml:strengthForm><witsml:mdStrengthForm uom="m">3654.5</witsml:mdStrengthForm><witsml:tvdStrengthForm uom="m">3547.5</witsml:tvdStrengthForm><witsml:diaCsgLast uom="in">7</witsml:diaCsgLast><witsml:mdCsgLast uom="m">4720</witsml:mdCsgLast><witsml:tvdCsgLast uom="m">3649</witsml:tvdCsgLast><witsml:presTestType>leak off test</witsml:presTestType><witsml:mdPlanned uom="m">-9999</witsml:mdPlanned><witsml:distDrill uom="m">-9999</witsml:distDrill><witsml:elevKelly uom="m">31</witsml:elevKelly><witsml:sum24Hr>Waited on weather. Not sufficient weather window for cleaning up well.</witsml:sum24Hr><witsml:forecast24Hr>Wait on weather.
When weather permits : pull deep set BTU plug.</witsml:forecast24Hr><witsml:ropCurrent uom="m/h">-9999</witsml:ropCurrent></witsml:statusInfo>
<witsml:extendedReport dTim="2011-10-04T00:00:00.000Z">Depth: 0. Waited on weather.</witsml:extendedReport >
<witsml:activity><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T06:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- waiting on weather</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited on weather. Not sufficient weather window for cleaning up well.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T06:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- waiting on weather</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited on weather. Not sufficient weather window for cleaning up well.
Simultaneously prepared for disconnecting EDP:
Bled off pressure in well from 80 bar to zero. Closed all valves in XT and LRP (except GSR). Disconnected all 3 electrical jumpers between EDP and LRP and parked on EDP. Bled off LP and HP pressure to XT. Disconnected hydraulic jumper from LRP and parked on LRP. Disconnected grease injection head hoses.</witsml:comments></witsml:activity>
</witsml:drillReport></witsml:drillReports>
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<witsml:drillReports version="1.4.0.0" xmlns:witsml="http://www.witsml.org/schemas/1series" xmlns:xsi="http://www.w3.org/2001/XMLSchema-instance" xsi:schemaLocation="http://www.witsml.org/schemas/1series http://www.npd.no/schema//DDRS/1series/WITSML_drillReport_profiled_schema_phase2.xsd"><witsml:documentInfo><witsml:documentName>Drill Report</witsml:documentName><witsml:owner>IIP</witsml:owner></witsml:documentInfo><witsml:drillReport><witsml:nameWell>NO 6506/12-P-1 BH</witsml:nameWell><witsml:nameWellbore>NO 6506/12-P-1 BH</witsml:nameWellbore><witsml:name>name</witsml:name><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:versionKind>normal</witsml:versionKind><witsml:createDate>2011-10-05T08:06:58.000Z</witsml:createDate>
<witsml:wellAlias><witsml:name>6506/12-P-1 BH</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellAlias>
<witsml:wellboreAlias><witsml:name>6506/12-P-1 BH</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellboreAlias><witsml:wellboreAlias><witsml:name>6644</witsml:name><witsml:namingSystem>NPD number</witsml:namingSystem></witsml:wellboreAlias>
<witsml:wellboreInfo><witsml:dTimPreSpud>2011-09-21T21:00:00.000Z</witsml:dTimPreSpud><witsml:dateDrillComplete>2011-09-21</witsml:dateDrillComplete><witsml:operator>Statoil</witsml:operator><witsml:drillContractor>Odfjell Drilling AS</witsml:drillContractor><witsml:rigAlias><witsml:name>DEEPSEA BERGEN</witsml:name><witsml:namingSystem>NPD Name</witsml:namingSystem></witsml:rigAlias><witsml:rigAlias><witsml:name>287983</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:rigAlias></witsml:wellboreInfo>
<witsml:statusInfo><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">6798.6</witsml:md><witsml:diaHole uom="in">0</witsml:diaHole><witsml:mdDiaHoleStart uom="m">4440</witsml:mdDiaHoleStart><witsml:strengthForm uom="g/cm3">1.6</witsml:strengthForm><witsml:mdStrengthForm uom="m">4376</witsml:mdStrengthForm><witsml:tvdStrengthForm uom="m">3909.5</witsml:tvdStrengthForm><witsml:diaCsgLast uom="in">5.5</witsml:diaCsgLast><witsml:mdCsgLast uom="m">6746.6</witsml:mdCsgLast><witsml:presTestType>formation integrity test</witsml:presTestType><witsml:mdPlanned uom="m">-9999</witsml:mdPlanned><witsml:distDrill uom="m">-9999</witsml:distDrill><witsml:elevKelly uom="m">23</witsml:elevKelly><witsml:sum24Hr>Laid down weak link bails to deck. Performed maintenance on BOP.</witsml:sum24Hr><witsml:forecast24Hr>Maintenance on BOP. WOW for running BOP.
Operational target tomorrow at 06:00; WOW for running BOP.</witsml:forecast24Hr><witsml:ropCurrent uom="m/h">-9999</witsml:ropCurrent></witsml:statusInfo>
<witsml:fluid><witsml:type>Packer fluid</witsml:type><witsml:dTim>2011-10-03T23:00:00.000Z</witsml:dTim><witsml:md uom="m">-9999</witsml:md><witsml:presBopRating uom="bar">690</witsml:presBopRating ><witsml:mudClass>water based</witsml:mudClass><witsml:density uom="g/cm3">1.11</witsml:density><witsml:pv uom="mPa.s">-9999</witsml:pv><witsml:yp uom="Pa">-9999</witsml:yp></witsml:fluid>
<witsml:porePressure><witsml:readingKind>measured</witsml:readingKind><witsml:equivalentMudWeight uom="g/cm3">1.06</witsml:equivalentMudWeight><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">4376</witsml:md></witsml:porePressure>
<witsml:extendedReport dTim="2011-10-04T00:00:00.000Z">Depth: 0. Performed maintenance on BOP. Changed UAP element.
Meanwhile: Changed out chicksan piping on rig floor. Installed pipe handler on top drive.</witsml:extendedReport >
<witsml:activity><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T02:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>completion -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Rigged down weak link bail system from rig floor.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T02:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T06:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>completion -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Performed maintenance on BOP. Changed to 9 5/8&quot; LPR.
Meanwhile: Disconnected pipe handler, upper and lower IBOP and saver sub from top drive for NDT testing. Checked main shaft and solid body elevator. Checked fluid level on ruckers.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T06:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>completion -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Performed maintenance on BOP. Pressure tested BOP on stump to 20/485 bar for 5/10 min. Found UAP leaking. Changed UAP element.
Meanwhile: Continued NDT of top drive components. Installed new upper and lower IBOP valves on top drive. Repaired hydraulic hoses on pipe handler. Changed out chicksan piping on rig floor. Greased kill and choke manifold. Checked fluid level on ruckers. Checked marine riser dogs.</witsml:comments></witsml:activity>
</witsml:drillReport></witsml:drillReports>
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<witsml:drillReports version="1.4.0.0" xmlns:witsml="http://www.witsml.org/schemas/1series" xmlns:xsi="http://www.w3.org/2001/XMLSchema-instance" xsi:schemaLocation="http://www.witsml.org/schemas/1series http://www.npd.no/schema//DDRS/1series/WITSML_drillReport_profiled_schema_phase2.xsd"><witsml:documentInfo><witsml:documentName>Drill Report</witsml:documentName><witsml:owner>IIP</witsml:owner></witsml:documentInfo><witsml:drillReport><witsml:nameWell>NO 6608/10-C-4 AH</witsml:nameWell><witsml:nameWellbore>NO 6608/10-C-4 AH</witsml:nameWellbore><witsml:name>name</witsml:name><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:versionKind>normal</witsml:versionKind><witsml:createDate>2011-10-05T08:07:51.000Z</witsml:createDate>
<witsml:wellAlias><witsml:name>6608/10-C-4 AH</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellAlias>
<witsml:wellboreAlias><witsml:name>6608/10-C-4 AH</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellboreAlias><witsml:wellboreAlias><witsml:name>4826</witsml:name><witsml:namingSystem>NPD number</witsml:namingSystem></witsml:wellboreAlias>
<witsml:wellboreInfo><witsml:dTimSpud>2003-11-15T00:00:00.000Z</witsml:dTimSpud><witsml:dateDrillComplete>2003-12-10</witsml:dateDrillComplete><witsml:operator>Statoil</witsml:operator><witsml:drillContractor>Island Offshore Management</witsml:drillContractor><witsml:rigAlias><witsml:name>ISLAND WELLSERVER</witsml:name><witsml:namingSystem>NPD Name</witsml:namingSystem></witsml:rigAlias><witsml:rigAlias><witsml:name>404470</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:rigAlias></witsml:wellboreInfo>
<witsml:statusInfo><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">-9999</witsml:md><witsml:diaHole uom="in">0</witsml:diaHole><witsml:diaCsgLast uom="in">7</witsml:diaCsgLast><witsml:mdCsgLast uom="m">3617</witsml:mdCsgLast><witsml:tvdCsgLast uom="m">2901</witsml:tvdCsgLast><witsml:presTestType>formation integrity test</witsml:presTestType><witsml:mdPlanned uom="m">-9999</witsml:mdPlanned><witsml:distDrill uom="m">-9999</witsml:distDrill><witsml:elevKelly uom="m">3</witsml:elevKelly><witsml:sum24Hr>Performed RST log. Not able to get signals from RST tool after two passes. Decided to log caliper. Logged OOH with caliper. Lost signals from caliper at 1000 m MD. POOH. L/D BHA#2. Disconnected UTH. WOW, meanwhile in transit to Sandnessjøen.</witsml:sum24Hr><witsml:forecast24Hr>WOW, meanwhile in transit to Sandnessjøen. WOW.
Status at 06:00: WOW at quay in Sandnessjøen.</witsml:forecast24Hr><witsml:ropCurrent uom="m/h">-9999</witsml:ropCurrent></witsml:statusInfo>
<witsml:extendedReport dTim="2011-10-04T00:00:00.000Z">Depth: 0. WOW.
Meanwhile: Transit to Sandnessjøen.</witsml:extendedReport >
<witsml:activity><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T04:30:00.000Z</witsml:dTimEnd><witsml:md uom="m">3455</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Performed RST-D in IC mode from 3418-3375 m MD at 0.5 m/min. Repeated logging pass. After second logging pass not able to get signals from RST tool.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T04:30:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T06:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">3455</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>equipment failure</witsml:stateDetailActivity><witsml:comments>Troubelshot RST tool. Not able to get signals. Decided to continue with caliper logging.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T06:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T10:30:00.000Z</witsml:dTimEnd><witsml:md uom="m">3455</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Performed caliper logging from 3455 m to 3415 m MD with 4.5 m/min. RIH to 3455 m MD. Performed caliper logging from 3455 m to 1021 m 10 m/min. WHP 118 bar. Annulus pressure 30 bar. Lost communication with caliper.
Meanwhile: Norne pressured up annulus pressure on D-1 to 60 bar. Performed survey with ROV on D-1. No visual leaks observed.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T10:30:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T13:30:00.000Z</witsml:dTimEnd><witsml:md uom="m">1000</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>equipment failure</witsml:stateDetailActivity><witsml:comments>Troubleshot signals from BHA while POOH. Pulled BHA into toolcatcher.
Meanwhile: Closed MV#42(230 Nm, 23 turn)</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T13:30:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T16:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">371</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>equipment failure</witsml:stateDetailActivity><witsml:comments>Closed UPIV and LPIV. Flushed stack with 800 ltr MEG. Inflow tested LPIV 70 bar/10 min. Inflow tested UPIV 345 bar/10 min.
Meanwhile: Established GW 2 and 4. Deployed PCH RT.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T16:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T18:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>equipment failure</witsml:stateDetailActivity><witsml:comments>Retrieved PCH and BHA to surface. Inspected and L/D BHA.
Meanwhile: Closed AMV, AP 50 bar. Closed DHSV. Connected Norne to SEM A.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T18:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T19:30:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>workover -- bop/wellhead equipment</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Prepared to disconnect UTH. Disconnected UTH and retrieved same to surface.
Meanwhile: Seafastened equipment on deck.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T19:30:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>interruption -- waiting on weather</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>WOW, meanwhile in transit to Sandnessjøen, ETA 08:00</witsml:comments></witsml:activity>
</witsml:drillReport></witsml:drillReports>
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