34 10-A-40.xml
9.46 KB
<witsml:drillReports version="1.4.0.0" xmlns:witsml="http://www.witsml.org/schemas/1series" xmlns:xsi="http://www.w3.org/2001/XMLSchema-instance" xsi:schemaLocation="http://www.witsml.org/schemas/1series http://www.npd.no/schema//DDRS/1series/WITSML_drillReport_profiled_schema_phase2.xsd"><witsml:documentInfo><witsml:documentName>Drill Report</witsml:documentName><witsml:owner>IIP</witsml:owner></witsml:documentInfo><witsml:drillReport><witsml:nameWell>NO 34/10-A-40</witsml:nameWell><witsml:nameWellbore>NO 34/10-A-40</witsml:nameWellbore><witsml:name>name</witsml:name><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:versionKind>normal</witsml:versionKind><witsml:createDate>2011-10-05T08:03:40.000Z</witsml:createDate>
<witsml:wellAlias><witsml:name>34/10-A-40</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellAlias>
<witsml:wellboreAlias><witsml:name>34/10-A-40</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellboreAlias><witsml:wellboreAlias><witsml:name>2070</witsml:name><witsml:namingSystem>NPD number</witsml:namingSystem></witsml:wellboreAlias>
<witsml:wellboreInfo><witsml:dTimSpud>1993-04-30T00:00:00.000Z</witsml:dTimSpud><witsml:operator>Statoil</witsml:operator><witsml:drillContractor>Aker Solution Services</witsml:drillContractor><witsml:rigAlias><witsml:name>GULLFAKS A</witsml:name><witsml:namingSystem>NPD Name</witsml:namingSystem></witsml:rigAlias><witsml:rigAlias><witsml:name>271833</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:rigAlias></witsml:wellboreInfo>
<witsml:statusInfo><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">-9999</witsml:md><witsml:diaHole uom="in">0</witsml:diaHole><witsml:mdDiaHoleStart uom="m">547</witsml:mdDiaHoleStart><witsml:diaCsgLast uom="in">5</witsml:diaCsgLast><witsml:mdCsgLast uom="m">4949</witsml:mdCsgLast><witsml:tvdCsgLast uom="m">1860</witsml:tvdCsgLast><witsml:mdPlanned uom="m">-9999</witsml:mdPlanned><witsml:distDrill uom="m">-9999</witsml:distDrill><witsml:elevKelly uom="m">82</witsml:elevKelly><witsml:sum24Hr>Waited for logging operation in well A-10. RIH with BHA# 1 Tractor and RST to 475 m. WL cabin and grease Skid shutt down. POOH fom 475 m. Statoil fire & gas tested and solved system for EL. WL equipment.</witsml:sum24Hr><witsml:forecast24Hr>RIH with BHA# 1 Tractor and RST. Log RST - D in Brent: 4340 - 3840 m and in Cook: 3720 - 3380 m. </witsml:forecast24Hr><witsml:ropCurrent uom="m/h">-9999</witsml:ropCurrent></witsml:statusInfo>
<witsml:extendedReport dTim="2011-10-04T00:00:00.000Z">Depth: 0. Equalized and opened HMV. Tested tractor and RST tool. Opened SV. WHP 92 bar. Depth: 2235. Ran in hole by gravity at 30 m/min lost weight at 2235 m. PU 50 m every 400 m (AWS procedure for new cable) Depth: 4280. Activated tractor and RIH from 2235 m to 4000 m 06:00. PU 50 m every 400 m (AWS procedure for new cable). Had to make 3 attempts to pass through straddle at 3548,5 m.</witsml:extendedReport >
<witsml:activity><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T06:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- wait</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited for logging operation in well A-10 to be completed. Common Slb acquisition computer. Meanwhile held A - standard / pre-job meeting with involved personnel on night shift.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T06:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T08:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- wait</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited for logging operation in well A-10 to be completed. Common Slb acquisition computer.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T08:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T09:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Performed A - standard / pre-job meeting with involved personnel on day shift.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T09:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T13:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- wait</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited for logging operation in well A-10 to be completed. Common Slb acquisition computer.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T13:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T15:45:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- wait</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Waited for logging operation in well A-10 to be completed. Common Slb acquisition computer.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T15:45:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T16:45:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Performed communication checks on logging tools. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T16:45:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T18:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Leaktested lubricator to 20/345 bar for 5/10 min with 100 % MEG. Opened HMV. WHP 93,8 bar. Pumped 50 ltr 100% MEG to equalize DHSV. Pumped 4 m3 of base oil. Openes swab. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T18:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T19:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Ran in hole by gravity at 30 m/min to 475 m. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T19:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T19:35:00.000Z</witsml:dTimEnd><witsml:md uom="m">475</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Winch cabin and unit for grease supply shut down. Loosed electric power due to gas alarm in D-21. AWS contacted SKR. Pressured up stuffing box to keep well control.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T19:45:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T20:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Gas alarm in D-21 cleared out. Electric power turned on. POOH from 475 m to surface. Closed SV and HMV.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T20:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T22:30:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Evaluated situation. Discussed situation w/ Statoil fire & gas prod dep. and electrician for sorting out why override of ignitionsource disconnection system failed.
</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T22:30:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Statoil fire & gas tested system for electric WL equipment. Solved the reason for cabin and grease loosed electric power shut down .Override of ignitionsource disconnection system for WL cabin was not activated on switchboard 17 - EN01.</witsml:comments></witsml:activity>
</witsml:drillReport></witsml:drillReports>