6506 12-P-1 BH.xml 5.5 KB
<witsml:drillReports version="1.4.0.0" xmlns:witsml="http://www.witsml.org/schemas/1series" xmlns:xsi="http://www.w3.org/2001/XMLSchema-instance" xsi:schemaLocation="http://www.witsml.org/schemas/1series http://www.npd.no/schema//DDRS/1series/WITSML_drillReport_profiled_schema_phase2.xsd"><witsml:documentInfo><witsml:documentName>Drill Report</witsml:documentName><witsml:owner>IIP</witsml:owner></witsml:documentInfo><witsml:drillReport><witsml:nameWell>NO 6506/12-P-1 BH</witsml:nameWell><witsml:nameWellbore>NO 6506/12-P-1 BH</witsml:nameWellbore><witsml:name>name</witsml:name><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:versionKind>normal</witsml:versionKind><witsml:createDate>2011-10-05T08:06:58.000Z</witsml:createDate>
<witsml:wellAlias><witsml:name>6506/12-P-1 BH</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellAlias>
<witsml:wellboreAlias><witsml:name>6506/12-P-1 BH</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellboreAlias><witsml:wellboreAlias><witsml:name>6644</witsml:name><witsml:namingSystem>NPD number</witsml:namingSystem></witsml:wellboreAlias>
<witsml:wellboreInfo><witsml:dTimPreSpud>2011-09-21T21:00:00.000Z</witsml:dTimPreSpud><witsml:dateDrillComplete>2011-09-21</witsml:dateDrillComplete><witsml:operator>Statoil</witsml:operator><witsml:drillContractor>Odfjell Drilling AS</witsml:drillContractor><witsml:rigAlias><witsml:name>DEEPSEA BERGEN</witsml:name><witsml:namingSystem>NPD Name</witsml:namingSystem></witsml:rigAlias><witsml:rigAlias><witsml:name>287983</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:rigAlias></witsml:wellboreInfo>
<witsml:statusInfo><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">6798.6</witsml:md><witsml:diaHole uom="in">0</witsml:diaHole><witsml:mdDiaHoleStart uom="m">4440</witsml:mdDiaHoleStart><witsml:strengthForm uom="g/cm3">1.6</witsml:strengthForm><witsml:mdStrengthForm uom="m">4376</witsml:mdStrengthForm><witsml:tvdStrengthForm uom="m">3909.5</witsml:tvdStrengthForm><witsml:diaCsgLast uom="in">5.5</witsml:diaCsgLast><witsml:mdCsgLast uom="m">6746.6</witsml:mdCsgLast><witsml:presTestType>formation integrity test</witsml:presTestType><witsml:mdPlanned uom="m">-9999</witsml:mdPlanned><witsml:distDrill uom="m">-9999</witsml:distDrill><witsml:elevKelly uom="m">23</witsml:elevKelly><witsml:sum24Hr>Laid down weak link bails to deck. Performed maintenance on BOP.</witsml:sum24Hr><witsml:forecast24Hr>Maintenance on BOP. WOW for running BOP.

Operational target tomorrow at 06:00; WOW for running BOP.</witsml:forecast24Hr><witsml:ropCurrent uom="m/h">-9999</witsml:ropCurrent></witsml:statusInfo>

<witsml:fluid><witsml:type>Packer fluid</witsml:type><witsml:dTim>2011-10-03T23:00:00.000Z</witsml:dTim><witsml:md uom="m">-9999</witsml:md><witsml:presBopRating  uom="bar">690</witsml:presBopRating ><witsml:mudClass>water based</witsml:mudClass><witsml:density uom="g/cm3">1.11</witsml:density><witsml:pv uom="mPa.s">-9999</witsml:pv><witsml:yp uom="Pa">-9999</witsml:yp></witsml:fluid>
<witsml:porePressure><witsml:readingKind>measured</witsml:readingKind><witsml:equivalentMudWeight uom="g/cm3">1.06</witsml:equivalentMudWeight><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">4376</witsml:md></witsml:porePressure>
<witsml:extendedReport  dTim="2011-10-04T00:00:00.000Z">Depth: 0. Performed maintenance on BOP. Changed UAP element.

Meanwhile: Changed out chicksan piping on rig floor. Installed pipe handler on top drive.</witsml:extendedReport >

<witsml:activity><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T02:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>completion -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Rigged down weak link bail system from rig floor.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T02:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T06:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>completion -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Performed maintenance on BOP. Changed to 9 5/8&quot; LPR.

Meanwhile: Disconnected pipe handler, upper and lower IBOP and saver sub from top drive for NDT testing. Checked main shaft and solid body elevator. Checked fluid level on ruckers.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T06:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>fixed</witsml:phase><witsml:proprietaryCode>completion -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Performed maintenance on BOP. Pressure tested BOP on stump to 20/485 bar for 5/10 min. Found UAP leaking. Changed UAP element.

Meanwhile: Continued NDT of top drive components. Installed new upper and lower IBOP valves on top drive. Repaired hydraulic hoses on pipe handler. Changed out chicksan piping on rig floor. Greased kill and choke manifold. Checked fluid level on ruckers. Checked marine riser dogs.</witsml:comments></witsml:activity>










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