33 12-B-42 AT2.xml 15.2 KB
<witsml:drillReports version="1.4.0.0" xmlns:witsml="http://www.witsml.org/schemas/1series" xmlns:xsi="http://www.w3.org/2001/XMLSchema-instance" xsi:schemaLocation="http://www.witsml.org/schemas/1series http://www.npd.no/schema//DDRS/1series/WITSML_drillReport_profiled_schema_phase2.xsd"><witsml:documentInfo><witsml:documentName>Drill Report</witsml:documentName><witsml:owner>IIP</witsml:owner></witsml:documentInfo><witsml:drillReport><witsml:nameWell>NO 33/12-B-42 A</witsml:nameWell><witsml:nameWellbore>NO 33/12-B-42 AT2</witsml:nameWellbore><witsml:name>name</witsml:name><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:versionKind>normal</witsml:versionKind><witsml:createDate>2011-10-05T08:00:47.000Z</witsml:createDate>
<witsml:wellAlias><witsml:name>33/12-B-42 A</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellAlias>
<witsml:wellboreAlias><witsml:name>33/12-B-42 AT2</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:wellboreAlias><witsml:wellboreAlias><witsml:name>5309</witsml:name><witsml:namingSystem>NPD number</witsml:namingSystem></witsml:wellboreAlias>
<witsml:wellboreInfo><witsml:dateDrillComplete>2007-01-05</witsml:dateDrillComplete><witsml:operator>Statoil</witsml:operator><witsml:drillContractor>DeepWell</witsml:drillContractor><witsml:rigAlias><witsml:name>STATFJORD B</witsml:name><witsml:namingSystem>NPD Name</witsml:namingSystem></witsml:rigAlias><witsml:rigAlias><witsml:name>271301</witsml:name><witsml:namingSystem>NPD code</witsml:namingSystem></witsml:rigAlias></witsml:wellboreInfo>
<witsml:statusInfo><witsml:dTim>2011-10-04T00:00:00.000Z</witsml:dTim><witsml:md uom="m">-9999</witsml:md><witsml:diaHole uom="in">0</witsml:diaHole><witsml:mdDiaHoleStart uom="m">4860</witsml:mdDiaHoleStart><witsml:strengthForm uom="g/cm3">1.75</witsml:strengthForm><witsml:mdStrengthForm uom="m">2094</witsml:mdStrengthForm><witsml:tvdStrengthForm uom="m">1829</witsml:tvdStrengthForm><witsml:diaCsgLast uom="in">5.5</witsml:diaCsgLast><witsml:mdCsgLast uom="m">4503.5</witsml:mdCsgLast><witsml:presTestType>formation integrity test</witsml:presTestType><witsml:mdPlanned uom="m">-9999</witsml:mdPlanned><witsml:distDrill uom="m">-9999</witsml:distDrill><witsml:elevKelly uom="m">77.8</witsml:elevKelly><witsml:sum24Hr>Performed time base log up from 760 m to surface. Bullheaded well with 100 m3 injection water.
RIH with EVO plug to 2286 m. Not able to activate tractor. POOH and not able to pass X-0 restriction to 812 m. Pumped 10 m3 injection water with RX in to the well. Worked string up and down. Still not able to pass restriction at 812 m. Set plug at 812 m. POOH. 
RIH and fished plug at 812 m. POOH.</witsml:sum24Hr><witsml:forecast24Hr>WOW due not able to brake lubricator and L/D BHA #4. L/D BHA #4. RIH with EVO dummy plug drift to 4500 m. POOH. RIH and install EVO plug a 4450 m. POOH.
Operational target tomorrow 06.00: Rig over to slick line. </witsml:forecast24Hr><witsml:ropCurrent uom="m/h">-9999</witsml:ropCurrent></witsml:statusInfo>



<witsml:extendedReport  dTim="2011-10-04T00:00:00.000Z">Depth: 0. WOW. Not able to break lubricator and L/D BHA #4 due to high wind. Depth: 0. Broke lubricator. L/D BHA #4 with EVO plug on deck. Observed 2 small marks on the shoulder top of plug. Depth: 0. Built new cabel head. Tested tractor and toolstring. Depth: 0. M/U BHA #5 ( dummy plug drift run). Stabbed lubricator. Leak tested QTS to 345 bar. Opened up well. WHP 33 bar.  Depth: 1300. RIH with BHA #5 to 1300 m.</witsml:extendedReport >

<witsml:activity><witsml:dTimStart>2011-10-03T00:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T01:15:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Performed time base log up from 760 m to surface with 15 m/min. Recorded station every 10 m for 15 seconds.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T01:15:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T02:15:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Closed in well. WHP 46 bar. Inflow tested HMV and swab. Broke lubricator. L/D BHA #2 on deck.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T02:15:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T04:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Tested tractor and toolstring signals. Prepared EVO plug toolstring on deck.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T04:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T04:45:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>M/U BHA #3 (EVO plug). Stabbed lubricator. Leak tested QTS to 345 bar. Opened up well. WHP 46 bar</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T04:45:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T06:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Bullheaded 3 m3 50/50 TEG, 17 m3 injection water with 750 lpm.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T06:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T08:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>Completed bullheading of well with a total of 100 m³ injection water. Maximum rate: 950 l/min. SIWHP dropped to 0 bar. Topped up with 3m³ 50/50% TEG mix. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T08:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T09:30:00.000Z</witsml:dTimEnd><witsml:md uom="m">2286</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>workover -- wire line</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>RIH w/ run #3 EVO plugg from 0 m to 2286 m, WHP 0 bar. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T09:30:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T10:15:00.000Z</witsml:dTimEnd><witsml:md uom="m">2286</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>equipment failure</witsml:stateDetailActivity><witsml:comments>Attempted several times to activate tractor. No go. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T10:15:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T12:30:00.000Z</witsml:dTimEnd><witsml:md uom="m">812</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>equipment failure</witsml:stateDetailActivity><witsml:comments>POOH from 2286 m. Hung up in SPM at 1388 m. Worked string free from restriction. Continued POOH. Hung up in X/O at 812 m. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T12:30:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T13:10:00.000Z</witsml:dTimEnd><witsml:md uom="m">812</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>stuck equipment</witsml:stateDetailActivity><witsml:comments>Attempted several times to pass restriction without success. Pulled up to 2500 lbs on surface. Also stuck for downwards movement. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T13:10:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T14:30:00.000Z</witsml:dTimEnd><witsml:md uom="m">812</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>stuck equipment</witsml:stateDetailActivity><witsml:comments>Mixed 10 m³ injection water with 2% RX - 72 friction reducer. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T14:30:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T16:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">812</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>stuck equipment</witsml:stateDetailActivity><witsml:comments>Lined up and pumped 1 m³ TEG mix, 10 m³ inj. water with 2% RX, 4 m³ inj. water og 1 m³ TEG mix.
SIWHP before pumping 34 bar. Max rate: 150 l/min. SIWHP after pumping 0 bar. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T16:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T17:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">812</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>stuck equipment</witsml:stateDetailActivity><witsml:comments>Pulled 2300 lbs on surface. Still not able to pass restriction. Set plug with midt packer element at 811 m. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T17:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T17:30:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>stuck equipment</witsml:stateDetailActivity><witsml:comments>POOH from 812 m to surface.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T17:30:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T18:30:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>stuck equipment</witsml:stateDetailActivity><witsml:comments>Closed in X-mas tree. WHP 10 bar. Inflow tested HMV and swab. Broke lubricator. L/D BHA #3. Observed 1 stuck wheel on tractor.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T18:30:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T19:45:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>stuck equipment</witsml:stateDetailActivity><witsml:comments>Built new cabel head. M/U BHA #4( pull EVO plug). Stabbed lubricator and leak tested QTS to 345 bar. Opened up well. WHP 22 bar.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T19:45:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T20:15:00.000Z</witsml:dTimEnd><witsml:md uom="m">800</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>stuck equipment</witsml:stateDetailActivity><witsml:comments>RIH with BHA #4 to 800 m. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T20:15:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T20:45:00.000Z</witsml:dTimEnd><witsml:md uom="m">800</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>stuck equipment</witsml:stateDetailActivity><witsml:comments>Pumped up tubing above plug to 40 bar.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T20:45:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T21:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">812</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>stuck equipment</witsml:stateDetailActivity><witsml:comments>RIH from 800 m to 812 m and latched on EVO plug. Equalized plug. WHP dropped to 15 bar. Jarred up 1 stroke plug free.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T21:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T21:30:00.000Z</witsml:dTimEnd><witsml:md uom="m">800</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>stuck equipment</witsml:stateDetailActivity><witsml:comments>POOH from 812 m to 800 m. Waited 30 min for plug element to retrack.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T21:30:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T22:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>stuck equipment</witsml:stateDetailActivity><witsml:comments>POOH from 800 m to surface. </witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T22:00:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-03T22:30:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- other</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>stuck equipment</witsml:stateDetailActivity><witsml:comments>Closed in X-mas tree. WHP 10 bar. Inflow tested HMV and swab.</witsml:comments></witsml:activity><witsml:activity><witsml:dTimStart>2011-10-03T22:30:00.000Z</witsml:dTimStart><witsml:dTimEnd>2011-10-04T00:00:00.000Z</witsml:dTimEnd><witsml:md uom="m">0</witsml:md><witsml:phase>wire line</witsml:phase><witsml:proprietaryCode>interruption -- waiting on weather</witsml:proprietaryCode><witsml:state>ok</witsml:state><witsml:stateDetailActivity>success</witsml:stateDetailActivity><witsml:comments>WOW. Not able to break lubricator and L/D BHA #4 due to high wind.</witsml:comments></witsml:activity>










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