<sum24Hr>RIH tag 7 3/4" landing collar at 10629ft. Test csg to 3500psi OK. Slip & Cut drilling line. Light drilling of cement from 10631ft to float collar at 10702ft. Drill float, observed rapid increase in return flow. Close in well observe pressures.</sum24Hr>
<forecast24Hr>Drill shoe track, Drill Tor formation.</forecast24Hr>
<comments>Displace well from 12.7 to 9.5 ppm Vesatec OBM. With 265gpm, 1700-2800psi.Meanwhile drill 3 ft cmt and Landing Collar at 10630ft, with 60 rpm 3-10 wob 60 rpm 9 kftlbs.</comments>
<comments>Obseved sudden increase in return flow, drop in WOB, increase in SPP. Picked off BTM. Flowcheck, positiv flow. Close in well on upper pipe Ram and closed choke. Observed pressure. SICP at 20:05, 866psi. At 20:30, 1236psi. At 21:00 1260psi. At 22:00 1274psi. Pump slowly into pipe to open float valve to establish SIDPP. Stopped pump when confirmed 50psi increase on casing gauge. SICP 1320psi and SIDPP 1320psi. Calculate Kill mud to be 12.0ppg. Pit gain 1.5bbl. Prepare Kill mud. Kick taken at 10707ft MD 10153ft TVD.</comments>
<comments>Before start killing the well reduce SIDPP from 1320psi to 1270psi. Start pumping at 30spm holding csg press at 1270psi, ICP at 1740psi Pump kill fluid according to pump schedule from surface to Bit. FCP 640psi. Kill well using W&W method.</comments>
</activity>
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<dTim>2010-05-20T00:00:00.001Z</dTim>
<runNumber>3</runNumber>
<serviceCompany>Baker Atlas</serviceCompany>
<mdTopdatum="KB"uom="m">2133.6</mdTop>
<mdBottomdatum="KB"uom="m">2438.4</mdBottom>
<tvdTopdatum="KB"uom="m">1111</tvdTop>
<tvdBottomdatum="KBx"uom="m">1111</tvdBottom>
<tool>Acoustic</tool>
<tempBHSTuom="degC">111.1</tempBHST>
<eTimStaticuom="h">11.11</eTimStatic>
<mdTempTooluom="m">4588.1</mdTempTool>
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<dTim>2010-05-20T00:00:00.001Z</dTim>
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<serviceCompany>Baker Atlas</serviceCompany>
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<mdBottomdatum="KB"uom="m">2133.6</mdBottom>
<tool>Acoustic</tool>
<tempBHCTuom="degC">111.1</tempBHCT>
<mdTempTooluom="m">4566.2</mdTempTool>
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<dTim>2010-05-20T00:00:00.001Z</dTim>
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<serviceCompany>Baker Atlas</serviceCompany>
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<tool>Acoustic</tool>
<mdTempTooluom="m">5112.6</mdTempTool>
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<coreInfouid="uuuu">
<dTim>2010-05-20T00:00:00.001Z</dTim>
<coreNumber>1</coreNumber>
<mdTopdatum="KB"uom="m">1524</mdTop>
<mdBottomdatum="KB"uom="m">1828.8</mdBottom>
<tvdTopdatum="KB"uom="m">1462.309</tvdTop>
<tvdBottomdatum="KB"uom="m">1741.274</tvdBottom>
<lenRecovereduom="m">304.495</lenRecovered>
<recoverPcuom="%">99.9</recoverPc>
<lenBarreluom="m">230</lenBarrel>
<innerBarrelType>aluminum</innerBarrelType>
<coreDescription>testing core no 1 data for ERH</coreDescription>
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<coreInfouid="uuuu">
<dTim>2010-05-20T00:00:00.001Z</dTim>
<coreNumber>2</coreNumber>
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<lenRecovereduom="m">169.164</lenRecovered>
<recoverPcuom="%">55.5</recoverPc>
<lenBarreluom="m">180</lenBarrel>
<innerBarrelType>fiberglass</innerBarrelType>
<coreDescription>testing core no 2 data for ERH</coreDescription>
<description>Drilled out 7 3/4" float collar at 10704ft, observed rapid increase in the return flow. Increase in DP pressure and loss of WOB. Closed in well on upper pipe ram. observed pressures. SICP increased to 1230psi, Established SIDPP to 1230psi.Circulate 12.0 ppg kill fluid from surface to bit according to pumping schedule.Pump 2000 stks with pump pressure decreasing from ICP 1730 psi to FCP 640 psi at 30 spm.Pumped 500 stks past the bit and kill fluid above 7 3/4" PBR increase kill rate to 40 spm.New FCP 980psi. Gain/losses steady. No expanding gas. After 4500 stks observe slight gas increase after poor boy from 65 to 129 units. Well killed. Open BOP. Slight gain decreasing. Circulate with 285 gpm 2405 psi. ECD 12,3 steady, MWT in return 10.9 ppg for a short period. Circulate and condition mud to even weight of 12.ppg. Flow check well for 30 minutes. Well stable. Circulate b/u, no gas in returns. Kill operation completed.</description>
</controlIncidentInfo>
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<dTim>2010-05-20T16:00:00.001Z</dTim>
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<tvdTopdatum="KB"uom="m">3187.714</tvdTop>
<description>Preliminary stratigraphy test text as</description>